Fault / Alarm
F0031
Main control cannot set a
Communication
communication link with the plug-
Fault with Plug-in
in module.
Module
F0033
Stator resistance setting fault
VVW Self-tuning
P0409.
Fault
F0048
Overload fault on the power pack
Overload on the
with IGBTs (3 s in 1.5xInom).
IGBTs
F0051
Overtemperature fault measured
IGBTs
on the temperature sensor of the
Overtemperature
power pack.
F0070
Overcurrent or short circuit on the
Overcurrent/Short
output, DC link or braking resistor.
Circuit
F0072
Motor Overload Fault (60 s in
Motor Overload
1.5xInom).
F0074
Ground overcurrent fault.
Note: This failure may be disabled
Ground Fault
by P0343.
F0076
There is an input phase fault or
Motor Conection
unbalanced 3 phase input power
Lost
supply.
F0078
Overtemperature fault measured
Motor
on the motor temperature sensor
Overtemperature
(Triple PTC) via analog input AIx or
digital input DIx.
F0079
Overtemperature fault measured
Motor
on the motor temperature sensor
Overtemperature
(Triple PTC) via dedicated circuitry
(dedicated input)
in the power scheme.
F0080
Fault related to the supervision
CPU Fault
algorithm.
(Watchdog)
F0084
Fault related to the automatic
Auto-diagnosis
identification algorithm of the
Fault
inverter hardware and plug-in
module.
F0091
External fault via DIx ("No External
External Fault
Fault" in P026x).
Quick Reference of Parameters, Alarms and Faults
Description
Possible Causes
Plug-in module is damaged.
Plug-in module is not properly connected.
Problem in the identification of the plug-in module; refer
to P0027 for further information.
Stator resistance value in P0409 does not comply with
the inverter power.
Motor connection error; turn off the power supply and
check the motor terminal box and the connections with
the motor terminals.
Motor power too low or too high in relation to the
inverter.
Inverter output overcurrent (>2xInom).
High ambient temperature around the inverter (>50 °C
(>122 °F)) and high output current.
Blocked or defective fan.
Heatsink is too dirty, preventing the air flow.
Short circuit between two motor phases.
Shor t circuit of the rheostatic braking resistor
connecting cables.
IGBTs module in short circuit or damaged.
Start with too short acceleration ramp.
Start with motor spinning without the Flying Start
function.
P0156, P0157 and P0158 setting is too low in relation
to the motor operating current.
Overload on the motor shaft.
Short circuit to the ground in one or more output
phases.
Motor cable capacitance too high, causing current
peaks in the output.
Bad motor connection to the drive.
Motor connection is broken.
Overload on the motor shaft.
Load cycle is too high (high number of starts and stops
per minute).
High ambient temperature around the motor.
Poor contact or short circuit (3 k9 < RPTC < 0k1).
Motor thermistor not installed.
Motor shaft is stuck.
Overload on the motor shaft.
Load cycle is too high (high number of starts and stops
per minute).
High ambient temperature around the motor.
Poor contact or short circuit (3 k9 < RPTC < 0 k1).
Motor thermistor not installed.
Motor shaft is stuck.
Electric noise.
Inverter firmware fault.
Poor contact in the connection between the main
control and the power pack.
Hardware not compatible with the firmware version.
Defect on the internal circuits of the inverter.
Wiring on DI1 to DI8 inputs are open or have poor
contact.
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