Ingersoll Rand QX Serie Manual De Usuario página 21

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Fault
Category
Code
Motor Controller
E-00
Fault
Motor Controller
E-01
Fault
Motor Controller
E-02
Fault
Motor Controller
E-0
Fault
Motor Controller
E-04
Fault
Motor Controller
E-05
Fault
Motor Controller
E-06
Fault
Motor Controller
E-0
Fault
Motor Controller
E-08
Fault
Motor Controller
E-09
Fault
Motor Controller
E-0A
Fault
E-0B,
Motor Controller
E-15
Fault
Motor Controller
E-0C
Fault
Motor Controller
E-0D
Fault
Motor Controller
E-0F
Fault
Motor Controller
E-10
Fault
48619852_ed2
Notes
Battery Fault
Invalid Hall State
I2T Fault
Motor Stall
Motor current
Over temperature
Current Offset
Shunt Calibration
Torque Offset Fault
Transducer Fault
Step Execution Timeout
Communication message timeouts
Over Torque limit
Over Angle Limit
Under Torque
Under Angle
Actions/Solutions
Replace battery.
Faulty HALL cable. Contact the IR Service
Center for service.
Check wireless settings using ICS to ensure
that tool's RF settings match with PCM. Also
confirm that the tool's ID is in the PCM's list.
Too much current being drawn over an
extended amount of time. Add a 10 second
delay between cycles to try and remedy. If it
is a very soft joint, try raising the shift down
point so that the majority of the cycle is run at
high speed.
Possible damaged electronics hardware.
Contact the IR Service Center for service.
Possible damaged electronics hardware.
Contact the IR Service Center for service.
Add a delay between cycles to allow time for
the tool to cool.
Possible damaged electronics hardware.
Contact the IR Service Center for service.
Faulty transducer or transducer wire. Contact
the IR Service Center for service.
Faulty transducer or transducer wire. Contact
the IR Service Center for service.
Faulty transducer or transducer wire. Contact
the IR Service Center for service.
Check the joint for stripped threads. If the
joint is a soft joint, extend the step timeout
parameter for the fastening configuration
being run.
Try pulling the trigger again.
Torque high limit is too low or the joint is too
hard for the fastening settings. For a hard
joint, try lowering the free speed to 0% and/
or lowering the shift down torque.
Check the joint for stripped threads. Angle
limit is too low or the joint is too soft for the
fastening settings
Torque low limit is too high or the user
released the trigger before the cycle was
complete. The user should keep the trigger
engaged until the cycle is complete.
Angle low limit is too high or the user
released the trigger before the cycle was
complete. The user should keep the trigger
engaged until the cycle is complete.
EN
EN-20
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